Commit e0183b97 authored by Mike Looijmans's avatar Mike Looijmans Committed by Jakub Kicinski

net: mdiobus: Prevent spike on MDIO bus reset signal

The mdio_bus reset code first de-asserted the reset by allocating with
GPIOD_OUT_LOW, then asserted and de-asserted again. In other words, if
the reset signal defaulted to asserted, there'd be a short "spike"
before the reset.

Here is what happens depending on the pre-existing state of the reset
signal:
Reset (previously asserted):   ~~~|_|~~~~|_______
Reset (previously deasserted): _____|~~~~|_______
                                  ^ ^    ^
                                  A B    C

At point A, the low going transition is because the reset line is
requested using GPIOD_OUT_LOW. If the line is successfully requested,
the first thing we do is set it high _without_ any delay. This is
point B. So, a glitch occurs between A and B.

We then fsleep() and finally set the GPIO low at point C.

Requesting the line using GPIOD_OUT_HIGH eliminates the A and B
transitions. Instead we get:

Reset (previously asserted)  : ~~~~~~~~~~|______
Reset (previously deasserted): ____|~~~~~|______
                                   ^     ^
                                   A     C

Where A and C are the points described above in the code. Point B
has been eliminated.

The issue was found when we pulled down the reset signal for the
Marvell 88E1512P PHY (because it requires at least 50ms after POR with
an active clock). Looking at the reset signal with a scope revealed a
short spike, point B in the artwork above.
Signed-off-by: default avatarMike Looijmans <mike.looijmans@topic.nl>
Reviewed-by: default avatarAndrew Lunn <andrew@lunn.ch>
Link: https://lore.kernel.org/r/20210202143239.10714-1-mike.looijmans@topic.nlSigned-off-by: default avatarJakub Kicinski <kuba@kernel.org>
parent 4160d9ec
......@@ -543,8 +543,8 @@ int __mdiobus_register(struct mii_bus *bus, struct module *owner)
mutex_init(&bus->mdio_lock);
mutex_init(&bus->shared_lock);
/* de-assert bus level PHY GPIO reset */
gpiod = devm_gpiod_get_optional(&bus->dev, "reset", GPIOD_OUT_LOW);
/* assert bus level PHY GPIO reset */
gpiod = devm_gpiod_get_optional(&bus->dev, "reset", GPIOD_OUT_HIGH);
if (IS_ERR(gpiod)) {
err = dev_err_probe(&bus->dev, PTR_ERR(gpiod),
"mii_bus %s couldn't get reset GPIO\n",
......@@ -553,8 +553,6 @@ int __mdiobus_register(struct mii_bus *bus, struct module *owner)
return err;
} else if (gpiod) {
bus->reset_gpiod = gpiod;
gpiod_set_value_cansleep(gpiod, 1);
fsleep(bus->reset_delay_us);
gpiod_set_value_cansleep(gpiod, 0);
if (bus->reset_post_delay_us > 0)
......
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